I had not used my buggy much in the last month as there seemed more important pressing matters that made having time for this very difficult. I also was aware that my steering box seemed to be acting rather oddly when it was turned full hard lock to the left . I had thought this was because of adjustment of the box but further examination proved that the front bearing on the box was shot. This had not been a new box I refurbished and the wear on it was an unknown factor.
I knew I would have to remove the Steering box and examine this further. The steering box was removed from the car by first undoing the steering column bolts on the universal disk. This released the column from the box. The tie rod ends where then undone and knocked out whilst the box was still bolted onto the beam. This made the process much easier. The box was then removed by undoing the two big bolts that hold the clamp around the beam . With the box removed I could see clearly that the box was unusable without serious repair:
The Video shows the extent of the wear on the main spindle of the old box.